人民长江
• 论文 • 上一篇 下一篇
位敏 陈利强 叶俊荣 崔冬冬
出版日期:
发布日期:
Online:
Published:
摘要: 部分河岸式溢洪道出口河道狭窄、曲折,岸坡陡峻,河床基础抗冲能力较差,采用挑流消能时挑射水流会砸落淘刷护坦、挑流鼻坎基础,危及下游岸坡稳定安全。为验证泄洪挑射水流形态及其对河床、岸坡的冲刷影响,以民乐河水库工程为例,通过水工模型试验进行分析并对挑流鼻坎体型进行优化。试验结果表明,溢洪道挑流鼻坎采用斜切坎配合折流器体型能有效改善挑射水流流态,对下游河床、岸坡的冲刷影响较小,可确保工程安全运行。
关键词: 溢洪道, 挑流消能, 斜切挑坎, 水工模型试验
Abstract:
The outlet channel of some river-bank spillways are characterized as narrow and zigzag with steep slopes and riverbed foundation of poor anti-scouring ability. When ski-jump energy dissipation is selected for this type of spillway, the ski-jump flow may hit and scour the apron and flip bucket foundation, which will endanger the downstream slope stability. In order to verify the deflecting flow hydraulic geometry and its scouring influence on riverbed and bank slope, the spillway of Minlehe Reservoir was taken as a case, hydraulic model test was carried out to optimize the shape of flip bucket. The test result shows that bevel-type flip bucket with deflector can improve the flow geometry and has little influence on downstream riverbed and slope, which will ensure the safety operation of the project.
Key words: spillway, ski-jump energy dissipation, bevel-type flip bucket, hydraulic model test
位敏 陈利强 叶俊荣 崔冬冬. 民乐河水库溢洪道挑流鼻坎体型优化试验研究[J]. 人民长江, doi: 10.16232/j.cnki.1001-4179.2016.19.016.
0 / / 推荐
导出引用管理器 EndNote|Ris|BibTeX
链接本文: http://www.rmcjzz.com/CN/10.16232/j.cnki.1001-4179.2016.19.016
http://www.rmcjzz.com/CN/Y2016/V47/I19/83